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UNITED STATES
DEPARTMENT OF LABOR
MINE SAFETY AND HEALTH ADMINISTRATION

DISTRICT 5

ACCIDENT INVESTIGATION REPORT
(UNDERGROUND COAL MINE)

FATAL ROOF FALL

Mine No. 2 (44-03808)
Navajo Coal Company
Wise, Wise County, Virginia

July 8, 1996

By

Harold J. Burnett
Coal Mine Safety and Health Inspector

David L.Fowler
Coal Mine Safety and Health Inspector

James R. Baker
Education and Training Specialist

Originating Office - Mine Safety and Health Administration
P.O. Box 560, Wise County Plaza, Norton, Virginia 24273
Ray McKinney, District Manager

GENERAL INFORMATION



Navajo Coal Inc., Mine No. 2 is located on Dotson Creek approximately two miles north of Wise, in Wise County, Virginia. The mine is opened by five drifts into the Norton Coalbed which ranges from 28 to 36 inches in height. Twenty-four miners are employed at the mine on two production shifts per day, five days a week with an average production of 350 tons of coal daily.

The mine operates one section, advancing five entries, utilizing a Jeffrey 102 Continuous Mining Machine and a continuous haulage system which consists of a 94L Bridge and 506 Bridge Carriers. Coal is transported to the surface by a belt conveyor system. The immediate mine roof consists of shale and sandstone which contains draw rock and/or small slips. The roof was being supported with 36 inch mechanically anchored bolts installed with two Fletcher Single Head, ATRS equipped roof bolting machines.

The roof control plan was adequate for the conditions encountered and persons interviewed were familiar with the requirements.

The MSHA approved training plan was also adequate for the conditions and mining system and records indicated that persons were being trained in accordance with this plan.

The mine Cleanup Program requires loose coal and coal dust to be cleaned up to the extent possible with the continuous mining machine, and after the continuous haulage system is moved out of the place and it is permanently supported, the remaining accumulations will be cleaned up with a scoop. (Two scoops were provided on the section to be used for this and other purposes.)

Navajo Coal Inc. assumed control of this operation in September, 1994. The principal officers of the corporation are:
Scott Moore....................President
Keith Ison........................Vice-President


The last safety and health (AAA) inspection conducted at this mine by the Mine Safety and Health Administration was completed on April 15, 1996.

DESCRIPTION OF THE ACCIDENT



On Monday, July 8, 1996, at 7:04 a.m., the day shift crew under the supervision of Freddie Williams, section foreman, and Danny Addington, superintendent, entered the mine and traveled to the 004 Section. Work progressed as normal until approximately 11:00 a.m. when the accident occurred. Jerry Wayne Adams, utility man, was assigned to operate the right side Fletcher RR1 Single Head Roof Bolting Machine in the absence of the regular roof bolting machine operator. Earlier in the shift, Adams was instructed to assist Jerry Strouth, roof bolting machine operator, on the left side of the section. Joe Addington, continuous mining machine operator, and Robert Woods, electrician, had completed mining the No. 2 Entry and had mined the second cut of the shift from the 4 Right Crosscut.

At approximately 10:40 a.m., Joe Addington and Woods moved the continuous mining machine into the face of the No. 4 Entry. At this time, Adams moved the right side roof bolting machine into the 4 Right Crosscut to begin roof bolting operations. A line curtain was installed on the right side of the No. 4 Entry to assist in ventilation while coal was being mined. The line curtain was installed across the opening of the 4 Right Crosscut. After mining the No. 4 Entry, Joe Addington and Woods moved the continuous mining machine into the last open crosscut of the No. 4 Entry for the purpose of servicing the machine.

At approximately 11:00 a.m., Joe Addington looked toward the curtain installed across the 4 Right Crosscut and could not see any movement or a reflection from Adams' cap lamp. Joe Addington then looked on the inby side of the line curtain and called for Adams several times. After receiving no response, he crawled to the location where Adams was working. Adams was on his knees at the operator's drill station trapped under a portion of fallen rock, which was approximately seven feet long, four feet wide and two to eight inches thick. Joe Addington called for help and Woods immediately came to assist him. Woods had to move the machine backward approximately three to four feet to facilitate recovery of Adams. (The fallen rock had completely cleared the roof bolting machine prior to moving the machine.) Several attempts to lift the rock failed. Other crew members, Dan Addington, Strouth, Jackie Wells, Jeff Pilkenton and Eric Mullins responded to Joe Addington's call for help. After retrieving a lifting jack from the section belt conveyor, the rock was lifted and Adams was recovered.

Surface personnel were notified and the local rescue squad was called. Eric Mullins, EMT-First Responder, examined Adams and began administering emergency treatment. Emergency treatment continued as Adams was transported to the surface. Adams was transported to the Wise Appalachian Regional Health Care Hospital by the Wise County Rescue Squad at 12:23 p.m., where he was pronounced dead.

PHYSICAL FACTORS INVOLVED IN THE ACCIDENT

  1. There were no eye witnesses to the accident and no contact between the victim and other members of the crew after he entered the No. 4 Right Crosscut. A line curtain installed up the right side of the No. 4 Entry prevented anyone from being able to see directly into the crosscut.

  2. Approximately four inches of loose coal and coal dust was present on the mine floor in the No. 4 Right Crosscut making it difficult to maneuver the roof bolting machine. The existence of mine floor irregularities interfered with the proper cleanup of this place with the continuous mining machine.

  3. The victim was found inby roof support under a portion of fallen rock which was approximately seven feet long, four feet wide and two to eight inches thick.

  4. The roof bolting machine was positioned with the rear of the machine angled toward the left rib with the operator's drill control station inby permanent roof support. The roof control plan requires the machine to be positioned with the rear of the machine angled toward the right rib as much as possible to obtain the best protection from the ATRS except while installing the roof bolts adjacent to the right rib. The crosscut being slightly off projections from the beginning resulted in the roof bolts being installed on a diagonal pattern which would make it more difficult to comply with this requirement. It appeared that the crosscut had been pulled to the right in order to connect with the No. 5 Entry which had not been advanced enough to allow cut through. The section loading point had been moved up to where the continuous haulage system could not be taken back to the No. 5 Entry face.

  5. The victim had completed the installation of the third bolt in the first row of the second cut from the crosscut. The next bolt in the installation process would have required him to maneuver the machine to install the first bolt in the second row adjacent to the left rib. During the interview session, the persons who recovered the victim from under the fallen rock could not recall if the ATRS was against the roof. However, the location of the ATRS and tram controls would have required the victim to be under supported roof while lowering the ATRS and/or maneuvering the machine. Therefore it is assumed that the ATRS was against the roof.

  6. Draw rock and/or small slips were present in the immediate mine roof but were being cut down with the continuous mining machine when possible. The primary roof support consisted of 36 inch mechanically anchored bolts on a four foot pattern with oversize bearing plates when needed.

  7. The victim was not performing his normal duties. He was classified as a utility man but was operating the roof bolting machine in the absence of the regular machine operator. However, records indicated that he had received task training as a roof bolting machine operator on 12/22/95 and had performed the task occasionally since then.

CONCLUSION



The accident occurred when the victim was operating the controls of the roof bolting machine from a location inby roof support. Other factors were:
  1. The roof bolting machine was positioned with the rear of the machine angled toward the left rib with the operator's drill control station inby permanent roof support.

  2. The construction of the roof bolting machine is such that if it is angled to the rear of the bolts being installed, with the rear to the left rib, the operator's controls are exposed to unsupported roof.

  3. Four inches of loose coal and coal dust on the mine floor in the 4 Right Crosscut made it difficult to maneuver the roof bolting machine.

ENFORCEMENT ACTIONS

  1. A 103(K) Order No. 3785391 was issued to insure the safety of any person until an investigation could be made.

  2. A 104(a) Citation No. 3355268, citing 30 CFR 75.202a was issued for a person working inby roof support.

  3. A 104(a) Citation No. 3355269, citing 30 CFR 75.220 was issued for a violation of the approved roof control plan. The roof bolting machine was not positioned in the manner required by the plan. The rear of the machine was not angled toward the right coal rib to afford the operator the most protection from the ATRS.




Respectfully submitted by:

Harold J. Burnett
Coal Mine Safety and Health Inspector

David L.Fowler
Coal Mine Safety and Health Inspector

James R. Baker
Education and Training Specialist


Approved by:

Ray McKinney
District Manager


Related Fatal Alert Bulletin:
Fatal Alert Bulletin Icon FAB96C19